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Mooney M20M - Engine Control Rigging

Mooney M20M
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SERVICE
AND
MAINTENANCE
MANUAL
M20M
MOONEY
AIRCRAFT
CORPORATION
A.
CHECK
AND
ADJUST
ENGINE
CONTROL
assembly
cushion
as
specified
in
Step
71-00-52,
A,
(2)
RIGGING
above
and
SECTION
61-20-00.
(1)
Operate
each
engine
control
through
full
(3)
Run
engine
until
170
to
1800
oil
temperature
range
of
travel;
check
that
it
operates
smoothly
and
is
obtained.
Slowly
apply
full
throttle
(propeller
and
contacts
the
stops
at
each
end
of
travel.
mixture
full
forward).
Observe
the
GSi~:0j0012-501*
readout
indicator
and
allow
the
intercooler
out
(2)
Check
each
control
at
the
instrument
panel
for
induction
air
temperature
to
stabilize.
Lycoming
SI
i~tard:06
inch
cushion
with
the
control
pushed
full
1187(G)
Alternate
Method)
(4)
Note
the
stabilized
intercoo\er
out
induction
CAUTION
air
temperature
on
GSE050012601
indicator
and
the
Do
not
force
vernier
controls
by
turning
knobs.
stabilized
manifold
pressure
on
a
calibrated
manifold
pressure
gauge
and
compare
with
chart
(Figure
71-3).
NOTE
If
manifold
pressure
at
the
observed
intercooler
out
Any
vernier
control
which
tends
to
creep
can
be
induction
air
temperature
falls
within
the
limits
indicated
tightened
by
loosening
the
housing
nut
on
the
in
the
chart
no
adjustment
of
the
density
controller
is
back
of
the
panel
and
tightening
the
face
nut
on
required.
However,
if
the
manifold
pressure
is
not
the
pilot
sideof
the
panel.
within
the
limits
shown
in
Figure
71-3,
the
density
controller
must
be
adjusted
as
described
in
Step
(5)
(3)
Adjust
controls
by
adjusting
rod
end
on
the
below
until
it
falls
within
the
required
band.
forward
end
of
the
control.
If
additional
adjustment
is
required,
the
control
arm
may
be
repositioned
to
adjust
(5)
The
dens~
controller
is
mounted
on
the
left
the
throttle
or
mixture,
aft
side
of
the
intercooler
(ref.
Figure
71-2).
Remove
lockwire
from
the
adjusting
fitting
and
by
means
of
a
(4)
Tighten
all
screws
and
resafety,
if
required.
small
wrench,
turnthe
square
head
of
the
fitting
clockwise
or
counterclockwise
to
accomplish
the
B.
FUEL
LINE
PURGE
adjustment.
Turning
the
screw
inward,
or
clockwise
will
increase
manifold
pressure;
tuming
it
counterclockwise
Disconnect
fuel
line
at
firewall.
Pump
out
will
decrease
manifold
pressure.
Be
careful
when
approximately
one
quart
of
fuel
using
the
auxiliary
fuel
reinstalling
safety
wire
to
avoid
turning
the
adjustment
boost
pump.
Select
the
opposite
tank
and
repeat.
fitting.
Reconnect
fuel
line.
CAUTION
C.
FUEL
BOOST
PUMP
THROTTLE
SWITCH
Turning
the
adjusting
fitting
1/16
turn
will
RIGGING
change
the
manifold
pressure
approximately
2
(1)
Turn
ignition
switch
OFF,
manual
fuel
boost
inches;
therefore,
CARE
MUST
BE
U(ERCISED
pump
switch
OFF,
mixture
at
idle
cutoff
and
aircraft
to
turn
the
screw
in
VERY
SMALL
increments
electrical
power
ON.
Push
throttle
full
NVD
(FULL
until
correct
adjustment
is
obtained.
POWER
POSITION);
verify
that
throttle
activated
fuel
(6)
If
discrepancies
in
the
controller
settings
boost
pump
switch
is
engaged
and
boost
pump
stays
between
ground
set
up
and
actual
flight
become
ON
while
the
throttle
is
pulled,
toward
idle,
until
0.38
to
evident,
then
the
following
procedure
shall
be
0.5
inches
from
the
full
MID
position.
accomplished.
Shut
the
engine
down
after
the
initial
(2)
Reposition
switch
and
actuator
arm
to
obtain
warm-up
for
4
to
5
minutes
to
allow
proper
heat
soak
of
the
above
criteria,
engine
components.
To
insure
that
temperatures
have
stabilized,
readings
and
adjustments
MUST
BE
made
(3)
Verify
that
BOOST
PUMP
annunciator
(BLUE
with
the
aircraft
cowling
installed.
Restart
engine
and
light)
is
illuminated.
run
(minimum
2
minutes)
until
induction
air
(4)
Verify
that
fuel
pressure
on
aircraft
gauge
temperature
has
stabilized.
does
not
exceed
55
PSI
and
does
not
drop
below
45
(7)
Recheck
all
idle
and
full
power
adjustments
to
PSI.
Adjust
or
replace
fuel
pump
as
required.
insure
that
they
meet
this
specification
and
readjust
if
D.
IDLE
ADJUSTMENT
necessary.
Verify
that
all
screws
are
tightened
and
resafety
if
required.
Refer
to
paragraph
71-00-51,
A.
and
B.
above.
E.
FULL
POWER
ADJUSTMENTS
(1)
Engine
running,
temperatures
and
pressures
F.
CLEAN
UP
in
normal
range
(GREEN)
slowly
apply
full
throttle
After
any
flight
checks
and
adjustments
are
complete,
(propeller
and
mixture
controls
FULL
FORWARD).
conduct
a
leak
check
of
all
connections.
CAUTION
Do
not
exceed
38.0
In.
Hg.
and
2600
RPM
under
any
circumstances
during
the
full
power
adjustment
process.
(2)
Verify
that
propeller
governor
will
allow
the
engine
to
operate
at
proper
static
RPM
to
obtain
2575
RPM
during
T/O
roll.
Refer
to
SECTION
61-20-30
for
propeller
governor
adjustment.
Recheck
control
cable
71-00-52
4-99
OLDWILLWAYNE

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