EasyManua.ls Logo

Honeywell BENDIX/KING KAP 140 - Page 94

Honeywell BENDIX/KING KAP 140
108 pages
To Next Page IconTo Next Page
To Next Page IconTo Next Page
To Previous Page IconTo Previous Page
To Previous Page IconTo Previous Page
Loading...
BENDIX/KING
KAP 140
Page 5--4
Revision 2, Dec/2002
CS:15574F02.IDU
ERR# TEXT MESSAGE(S) POSSIBLE FAILED UNIT(S)
DESCRIPTION OF ERROR
16 Timer failed KC 140
The processor failed the timer test on power up. Autopilot operation is disallowed.
20 Watchdog timed out KC 140
The watchdog was not reset in the allowed time period. This indicates a probable hardware
fault in the flight computer. Autopilot operation is disallowed.
25 Roll srv cmd over upper range KC 140
Preflight test failed due to improper response to roll servo command wraparound signal.
This indicates a probable failure in the roll servo command circuit or the analog to digital
input circuitry of the flight computer. Autopilot operation is disallowed.
26 Roll srv cmd below upper range KC 140
Preflight test failed due to improper response to roll servo command wraparound signal.
This indicates a probable failure in the roll servo command circuit or the analog to digital
input circuitry of the flight computer. Autopilot operation is disallowed.
27 Roll srv cmd over lower range KC 140
Preflight test failed due to improper response to roll servo command wraparound signal.
This indicates a probable failure in the roll servo command circuit or the analog to digital
input circuitry of the flight computer. Autopilot operation is disallowed.
28 Roll srv cmd below lower range KC 140
Preflight test failed due to improper response to roll servo command wraparound signal.
This indicates a probable failure in the roll servo command circuit or the analog to digital
input circuitry of the flight computer. Autopilot operation is disallowed.
29 Norm accel over 1g upper limit KC 140
Preflight test failed due to improper response of the accelerometer after self test. If this error
occurs in flight, it should be ignored. Otherwise, this indicates a probable failure in the
accelerometer or the associated circuitry of the flight computer. Pitch Axis operation is
disallowed.
30 Norm accel below 1g upper limit KC 140
Preflight test failed due to improper response of the accelerometer after self test. If this error
occurs in flight, it should be ignored. Otherwise, this indicates a probable failure in the
accelerometer or the associated circuitry of the flight computer. Pitch Axis operation is
disallowed.
31 Norm accel over tst upper limit KC 140, KS 270C
Preflight test failed due to improper response of the accelerometer during self test. This
indicates a probable failure in the accelerometer or the associated circuitry of the flight
computer. Pitch Axis operation is disallowed. NOTE: In --5201, --5402, and --7702 FCC
flavors, this error can be caused by missing or improper tach feedback from the pitch servo.

Related product manuals