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YASKAWA GA50U Series - Page 97

YASKAWA GA50U Series
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13 Troubleshooting
YASKAWA TOEPC71061752B GA500 Drive Installation & Primary Operation 97
Code Name Causes Possible Solutions
The acceleration time is too short. Calculate the torque necessary during
acceleration related to the load inertia
and the specified acceleration time.
Increase the values set in C1-01, C1-03,
C1-05, or C1-07 [Acceleration Times] to
get the necessary torque.
Increase the values set in C2-01 to C2-04
[S-Curve Characteristics] to get the
necessary torque.
Replace the drive with a larger capacity
model.
The drive is trying to operate a
specialized motor or a motor that
is larger than the maximum
applicable motor output of the
drive.
Examine the motor nameplate, the motor,
and the drive to make sure that the drive
rated current is larger than the motor
rated current.
Replace the drive with a larger capacity
model.
A magnetic contactor was
switched at the output.
Set the operation sequence to not turn ON or
OFF the magnetic contactor while the drive
is outputting voltage.
The V/f pattern settings are
incorrect.
Examine the ratios between the V/f
pattern frequency and voltage. Decrease
the voltage if it is too high compared to
the frequency.
Adjust E1-04 to E1-10 [V/f Pattern
Parameters]. For motor 2, adjust E3-04
to E3-10.
The torque compensation gain is
too large.
Decrease the value set in C4-01 [Torque
Compensation Gain] to make sure that the
motor does not stall.
Electrical interference caused a
problem.
Examine the control circuit lines, main
circuit lines, and ground wiring, and
decrease the effects of electrical
interference.
The gain during overexcitation
operation is too large.
Find the time when the fault occurs.
If the fault occurs at the same time as an
overexcitation operation, decrease n3-13
[OverexcitationBraking (OEB) Gain]
and consider the motor flux saturation.
The drive received a Run
command while the motor was
coasting.
Examine the sequence and input the Run
command after the motor fully stops.
Set b3-01 = 1 [Speed Search at Start
Selection = Enabled] or set H1-xx = 61,
62 [Speed Search from Fmax or Fref] to
input speed search commands from the
MFDI terminals.
In PM Control Methods, the
setting of the motor code is
incorrect.
Enter the correct motor code to E5-01
[PM Motor Code Selection] as specified
by the PM motor.
For specialized motors, refer to the motor
test report and set E5-xx [PM Motor
Settings] correctly.

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