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Inovance NICE1000 - Page 46

Inovance NICE1000
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Page 45 of 49
Version : 1.4
Date of issue : 03-07-14
2. The drive control board fails.
whether the power voltage is
normal. If not, adjust the power
input.
2. Contact the agent or Monarch
Err 13
E13
Output side
Phase failure
1. The output wiring of the main
circuit is loose.
2. The motor is damaged.
1. Check the wiring.
2. Check whether the contactor at
the output side is normal.
3. Eliminate the motor fault
4
Err 14
E14
Module
Overheated
1. The ambient temperature is too
high.
2. The fan is damaged.
3. The air channel is blocked.
1. Lower the ambient
temperature.
2. Clear the air channel.
3. Replace the damaged fan.
4. Check whether the installation
clearance of the controller
satisfies the requirement
5
Err 16
E16
Encoder
Fault
1. The start-up position is
incorrect.
2. The torque deviation is too
large.
3. The speed deviation is too
large.
1. Check the encoder circuit.
2. Turn off the output MCCB.
3. The current loop parameters are
too small.
4. The zero-point position is
incorrect. Perform motor auto
tuning again.
5. Reduce the load
5
Err 17
E17
Encoder signal
check
abnormal
The deviation of real-time angle
and reference angle of the 1387
encoder is too large.
1. Check whether the encoder is
normal.
2. Check whether the encoder
wiring is reliable and normal.
3. Check whether the PG card
wiring is proper.
4. Check whether the main unit
and control cabinet are grounded
well
5
Err 18
E18
Current
detection fault
Diver control Board is failed
Contact with agent or factory
5
Err 19
E19
Motor
tuning
fault
1. The motor cannot rotate
properly.
2. The motor auto tuning times
out.
3. The encoder for the PMSM
fails.
1. Enter the motor parameters
correctly.
2. Check the motor wiring and
whether phase loss occurs on the
contactor at the output side.
3. Check the feedback encoder
wiring and ensure that PPR of the
encoder is set properly.
4. Check whether the brake keeps
released during no-load auto-
tuning.
5. Check whether the inspection
button is released before the
PMSM with-load auto-tuning is
finished.
5
Err 20
E20
Rotary
encoder fault
1. Check whether the encoder
model matches the motor.
2. The encoder wiring is
incorrect.
1. Check whether F1-00 is set
correctly.
2. Check the encoder wiring.
3. Check whether the encoder is
5

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