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Omron SMARTSTEP 2 R88M-G Series - Page 306

Omron SMARTSTEP 2 R88M-G Series
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8-9
8-3 Troubleshooting
8
Troubleshooting
23 Encoder data error Occurs when the power
supply is turned ON or
during operation.
The encoder signal wir-
ing is incorrect.
Correct the wiring.
Noise on the encoder
wiring causes incorrect
operation.
Take measures against
noise on the encoder wir-
ing.
The power supply volt-
age for the encoder has
dropped (especially
when the cable is long.)
Provide the required en-
coder power supply volt-
age (5 VDC±5%).
24 Deviation counter
overflow
Occurs when the Ser-
vomotor does not ro-
tate even when
command pulses are
input.
The Servomotor power
wiring or the encoder wir-
ing is incorrect.
Correct the wiring.
The Servomotor is me-
chanically being held.
If the Servomotor shaft is
held by external force, re-
lease it.
Release the electromag-
netic brake.
Control PCB error. Replace the Servo Drive.
Occurs during high-
speed rotation.
The Servomotor power
wiring or the encoder wir-
ing is incorrect.
Correct the wiring.
Occurs when long com-
mand pulses are given.
Gain adjustment is insuf-
ficient.
Adjust the gain.
The acceleration and de-
celeration are too rapid.
Extend the acceleration
and deceleration times.
The load is too large. Reduce the load.
Select a suitable Servo-
motor.
Occurs during opera-
tion.
The setting for the Devia-
tion Counter Overflow
Level (Pn63) was ex-
ceeded.
Increase the setting of
Pn63.
Slow the rotation speed.
Reduce the load.
Extend the acceleration
and deceleration times.
26 Overspeed Occurs during high-
speed rotation.
The speed command in-
put is too large.
Set the command pulse
frequency to 500 kpps
max.
The setting for the Elec-
tronic Gear Ratio Numer-
ato
r (Pn46 o
r Pn47) is not
appropriate.
Set Pn46 and Pn47 so
that the command pulse
frequency is 500 kpps
max.
The maximum number of
rotations is exceeded
due to overshooting.
Adjust the gain.
Reduce the maximum
command speed.
The encoder wiring is in-
correct.
Correct the wiring.
Occurs when torque
limit switching is used.
The Overspeed Detec-
tion Level Setting (Pn70)
or No. 2 Overspeed De-
tection Level Setting
(Pn73) has been exceed-
ed.
If torque limit switching is
used, correctly set the al-
lowable operating speed
for Pn70 and Pn73.
Alarm
code
Error
Status when error
occurs
Cause Countermeasure

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