Operation instructions
SIPOS 5 PROFITRON, HiMod
Page 60 Y070.020/GB
7 Status and fault signals, diagnosis
7
Status and fault signals, diagnosis
No
Message Explanation Possible remedy
5
runtime error
3
After 3 % of the commissioning time, the
actuator has cover less than 0.5 % travel.
The positioning time is measured and sa-
ved for the set output speed for end position
adjustment.
Possible reasons:
■
Potentiometer contacts in the plug/ socket
connector were ejected.
■
Incorrect assembly and/or setting of the
potentiometer after an exchange.
■
Motor cable interrupted (motor is not
running).
■
Error during position recording (the gear
backlash between potentiometer and
central wheel is too small or too large: No
change of position is detected although
the motor is running).
■
Signaling gear ratio was changed
– Signaling gear turns in the opposite
direction or
– setting of the slide wheel (rev/stroke in
the signaling gear is to high).
■
Actuator is blocked (actuator cannot be
operated from position/end position).
■
Faulty potentiometer (fi lm is interrupted).
■
• Parameter for separate mounting
„>10m with fi lter“ not set.
■
Check valve, signalling gear, motor and
potentiometer!
■
Check „Sep. mounting“ parameter.
22
setp. inp. Error
1
This message is only possible for
(4 – 20 mA) live-zero setting.
Threshold I: > 21 mA or < 3.6 mA.
■
Increase or reduce current,
■
check input current!.
20
voltage error
1,4
Supply voltage/electronics fault. Replace electronics.
27
watchdog error
4
Watchdog error. Replace electronics.
___________________________
1
Automatically resetting error.
2
Further action by the operator required at the actuator.
3
Fault can be acknowledged, refer to chapter 7.1.
4
Service required, refer to chapter 8.1.