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ABB DCS 400 - Page 150

ABB DCS 400
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II K 6-28
Operating Instructions
Fault message
Fault no.
Definition /
Possible source
Param.
F 17 Tacho Polarity Fault
Tacho Polarity Fault
Polarity of feed back signal from
tacho generator incorrect.
Please check
the polarity of tacho gene-
rator cable
polarity of armature and field
cable
direction sense of rotation of
the motor
7.10
bit 0
F 18 Overspeed
Overspeed
The actual speed of motor too
high.
Possible causes:
Running in torque/current
controlled mode instead of
speed controlled.
Speed regulator parameters
are not correct (overshoot or
instability , see Parameter
Group 5)
Motor driven by external
load.
7.10
bit 1
F 19 Motor Stalled
Motor Stalled
Motor not turning at zero speed
level (Parameter Zero Speed
Lev (5.15)) with actual torque
higher than the torque limit (Pa-
rameter Stall Torque (3.17)) for
a time longer than the limiting
time (Parameter Stall Time
(3.18)).
Please check
all mechanical couplings of
the motor
the proper condition of load
current/torque limitation
parameter settings (Group
3)
7.10
bit 2
F 20 Communication Fault
see also A11
Communication Fault
if command location Parameter
2.02 is set to Fieldbus. Field-
bus communication errors ap-
pear if no messages have been
received for longer than the time
which is set in Parameter Comm
Fault Time (2.08) . If command
location is not Fieldbus Alarm
11 appears instead.
Please check the connection of
Fieldbus cable and check the
function of all Fieldbus devices
according to the values in Para-
meter Group 8
7.10
bit 3
Fault message
Fault no.
Definition /
Possible source
Param.
F 13 Field Overcurrent
Field Overcurrent
Field current has reached a limit
(Parameter Field Ov Cur Trip
(4.05)) that could damage the
motor.
Please check
the field related parameters
the resistance of the field
connections of the field
insulation level of cable and
field winding
7.09
bit 12
F 14 Armature
Overcurrent
Armature Overcurrent
Armature current higher than
value of Parameter 3.04 Arma-
ture current max . The problem
can be caused by a short circuit
in the armature circuit or a thyri-
stor is defective.
Please switch off the drive and
check
measure the resistance of
armature
all connections in the arma-
ture circuit
function of all thyristors
parameters of the Current
Controller (Group 3) for in-
stability.
7.09
bit 13
F 15 Armature
Overvoltage
Armature Overvoltage
The voltage of the armature has
grown higher than the value in
Parameter Arm Overv Trip
(1.09).
Possible problems:
Too low fault level set (con-
sider voltage overshoots) or
wrong nominal motor voltage
Too high field current, may-
be problems with field wea-
kening (see field parame-
ters)
Overshoot or instability of
speed/armature current con-
troller
Overspeed
7.09
bit 14
F 16 Speed Meas Fault
Speed Measurement Fault
The comparison of the speed
feed back signal from the tacho
generator or pulse encoder has
failed or overflow of analogue
input AITAC.
Please check
all connections of tacho ge-
nerator or
pulse encoder
encoder supply
converter connections - ar-
mature ciruit open?
7.09
bit 15

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