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Cessna 177 SERIES Service Manual

Cessna 177 SERIES
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11-35.
TROUBLE
SHOOTING
(Cont).
TROUBLE
PROBABLE
CAUSE REMEDY
HIGH
OIL
TEMPERATURE
Oil
congealed
in
cooler.
This
condition
can
occur
only
in
(CONT).
extremely
cold
temperatures.
If
congealing
is
suspected,
use
an
external
heater
or
a
heated
hangar
to
warm
the
congealed
oil.
OIL
LEAK
AT
FRONT
OF
Damaged
crankshaft
seal.
Replace.
ENGINE.
OIL
LEAK
AT
PUSH
ROD
Damaged
push
rod
housing oil
seal.
Replace.
HOUSING.
11-36.
FULL-FLOW
OIL
FILTER.
(Refer
to
figure
these
are generally
of
no
consequence
and
11-3.)
should
not
be
confused
with
particles
pro-
duced
by
impacting,
abrasion
or
pressure.
11-37.
DESCRIPTION.
An
external
oil
filter
may
be
Evidence
of
internal
damage
found
in the
oil
installed
on
the
engine.
The
filter
and
filter
adapter
filter
element
justifies
further
examination
replace
the
regular
engine
oil
pressure
screen
and
to
determine
the
cause.
cast
chamber
on
the
accessory
housing.
The
filter
adapter
incorporates
mounting
provisions
for
the
oil
f.
Wash
lid
(7),
hollow
stud
(12)
and
filter
can
(10)
cooler
bypass
valve
and
the
oil
temperature
sensing
in
solvent
and
dry
with
compressed
air.
bulb.
If
the
filter
element
should
become
clogged,
the
bypass
valve
allows
engine
oil
to
flow
to
the
en-
NOTES
gine
oil
passages.
When
installing
a
new
filter
element
(9),
it
11-38.
REMOVAL
AND
INSTALLATION.
(Refer
to
is
important
that
all gaskets
are
clean, lu-
figure
11-3.)
bricated
and
positioned
properly,
and
that
the
correct
amount
of
torque
is
applied
to
NOTE
the
hollow
stud
(12).
If
the
stud
is
under-
torqued,
oil
leakage
will
occur.
If
the
stud
Filter
element replacement
kits
are
avail-
is
over-torqued,
the
filter
can
might
possi-
able
from
the
Cessna
Service
Parts
Center.
bly
be
deformed,
again
causing
oil
leakage.
a.
Remove
engine
cowling
in
accordance
with
para-
*
Lubricate
all
rubber
grommets
in
the
new
graph
11-3.
filter
element,
lid
gaskets
and
metal
gas-
b.
Remove
both
safety
wires
from
filter
can
and
ket
with
clean
engine
oil
or
general
purpose
unscrew
hollow
stud
(12)
to
detach
filter
assembly
grease
before
installation.
Dry
gaskets
from
adapter
(2)
as
a
unit.
Remove
assembly
from
may
cause
false
torque
readings,
again
aircraft
and
discard
gasket
(5).
resulting
in
oil
leakage.
c.
Deleted.
*
Before
assembly,
place
a
straightedge
across
d.
Lift
lid
(7)
off
filter
can
(10)
and
discard
gasket
bottom
of
filter
can.
Check
for
distortion
or
(8).
out-of-flat
condition
greater
than
0.010
inch.
e.
Pull
filter
element
(9)
out
of
filter
can
(10).
Install
a
new
filter
can
if
either
of
these
con-
ditions
exist.
NOTE
*After installing
a
new
gasket
on
lid,
turn
lid
Before
discarding
removed
filter
element
(9),
over.
If
gaskets falls,
try
a
different
gasket
remove
the outer
perforated
paper
cover;
and
repeat
test.
If
this
gasket
falls
off,
in-
using
a
sharp
knife,
cut
through
the
folds
of
stall
a
new
lid.
the
filter
element
at
both
ends.
Then,
care-
fully unfold
the
pleated
element
and
examine
g.
Inspect
the
adapter
gasket
seat
for
gouges,
deep
the
material
trapped
in
the
element
for
evi-
scratches,
wrench
marks
and
mutilation.
If
any
of
dence
of
internal
engine
damage,
such
as
these
conditions
are
found,
install
a
new
adapter.
chips
or
particles
from
bearings.
In
new
or
h.
Place
a
new
filter
element
(9)
in
can
(10)
and
in-
newly
overhauled
engines,
some
small par-
sert
the
hollow
stud
(12)
with
a
new
metal
gasket
(11)
tides
or
metallic
shavings
might
be found,
in
place,
through
the
filter
can
and
element.
11-16
Change
4

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Cessna 177 SERIES Specifications

General IconGeneral
ManufacturerCessna
Engine TypePiston
Wingspan35 ft 6 in (10.82 m)
Seating Capacity4
Number Built4, 295
EngineLycoming O-360
Horsepower180 hp
Maximum Takeoff Weight2, 500 lb (1, 134 kg)

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