Goodrive35 inverters Fault tracking
250
The baud rate setting is
incorrect.
Fault occurs to the
communication wiring.
The communication address
is wrong.
There is strong interference
to the communication.
Set proper baud rate
Check the communication
connection distribution
Set proper communication
address.
Chang or replace the connection
distribution or improve the
anti-interference capability.
The connection of the control
board is not good
Assistant power is bad
Hall components is broken
The modifying circuit is
abnormal.
Check the connector and
repatch
Change the Hall
Change the main control panel
The motor capacity does not
comply with the inverter
capability
The rated parameter of the
motor does not set correctly.
The offset between the
parameters from autotune
and the standard parameter
is huge
Autotune overtime
Change the inverter mode
Set the ratedparameter
according to the motor name
plate
Empty the motor load and
reindentify
Check the motor connection and
set the parameter.
Check if the upper limit
frequency is above 2/3 of the
rated frequency.
Error of controlling the write
and read of the parameters
Damage to EEPROM
Press STOP/RST to reset
Change the main control panel
PID feedback
outline fault
PID feedback offline
PID feedback source
disappear
Check the PID feedback signal
Check the PID feedback source