Because of apron distance not possible to move down more!
The min. distance from the shaft pit which is allowed to be reached with an out-folded apron has been
reached during downward travel.
The controller initiates an emergency stop
- limit has been reached
- parameters not set correctly
- retract the hinged apron, retract the telescopic apron
- check parameters Menu -> Parameter -> Input/Output -> In car -> Auto hinged apron ->
Dist.limit to drive
800 + Ok / Recall / Reset
3 sec. after the beginning of travel, the controller checks whether the brakes are released; that is in case
of an error the input Brake3 is still applied.
The controller switches into “out-of-order” mode.
- brake activation does not function properly (refer to wiring diagram)
- brake shoe contact is not set up correctly
- wiring not correct
- Brake MCB (FBR)
- defective input
- see causes
- check input on the status page (BR3)
If the input should be defective it can be parameterized to another available I/O any time.
800 + Ok / Recall / Reset
3 sec. after the termination of travel, the controller checks whether the brakes are closed; that is in case
of an error the input Brake3 is not applied.
The controller switches into “out-of-order” mode.
- brake activation does not function properly (refer to wiring diagram)
- brake shoe contact is not set up correctly
- wiring not coorect
- defective input
- see causes
- check input on the status page (BR3)
If the input should be defective it can be parameterized to another available I/O any time.