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YASKAWA SGM-A3 - Page 407

YASKAWA SGM-A3
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6.2 Troubleshooting
395
Status When Alarm Occurred
A
During servomotor
operation
Overflow during
high-speed opera-
tion
No feedback pulse
returned after refer-
ence pulse input.
Normal operation
but overflow when
large reference in-
put.
At control power ON
B
,
F
C
,
D
,
E
F
Cause Remedy
A Servomotor wiring incorrect.
Check and correct wiring. (Check A-, B-,
Ch
2CN )
B Encoder wiring incorrect (disconnection,
short, power supply, etc.)
g
(
,
,
C-phase pulses correct at 2CN.)
C Servopack adjustment incorrect Increase speed loop gain (Cn-04) and/or
position loop gain (Cn-1A).
D Servomotor overloaded Reduce load torque and inertia. Otherwise,
replace with larger capacity servomotor.
E Position reference pulse frequency too
high
Decrease reference pulse frequency.
Use smoothing function.
Change electronic gear ratio.
F Circuit board (1PWB) defective. Replace Servopack.
D Display and Outputs
Digital Operator
Di l
d
Alarm Output
g
p
Display and
Alarm
Name
Alarm Code Output
Alarm Output
Al
arm
N
ame
ALO1 ALO2 ALO3
p
A.40
Overvoltage
OFF OFF ON OFF
OFF: Output transistor is OFF
ON: Output transistor is ON
Status When Alarm Occurred
A
,D
During servomotor
operation
During motor
deceleration
During normal
operation
At main circuit power ON
B
,
C
,D
E
At control power ON
F
6

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