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Building Technologies   Basic documentation LMV37.4...  CC1P7546en 
 12 Fan control  17.12.2018 
 
6.  Close the standardization 
When standardization is successfully completed, reset parameter 641 to 0. 
If standardization was not successful, parameter 641 assumes a negative value. 
 
No. Parameter 
641 
Control of VSD’s speed standardization 
Error diagnostics of negative values (refer to error 82) 
0 = no speed standardization 
1 = speed standardization active 
 
The value provides information on the cause of fault: 
 
Value  Error  Remedy 
-1  Timeout of standardization (VSD’s ramp down 
time too long) 
Timeout at the end of standardization during ramp down 
of VSD. 
→ VSD ramp time settings are not shorter than those of 
the LMV37.4 (parameter 523). 
-2  Storage of standardized speed not  
successful 
Error during storage of standardized speed  
 lock the LMV37.4 and reset it again, repeat 
standardization 
-3  Line interruption speed sensor  LMV37.4 receives no pulses from the speed sensor. 
 
1.  Motor does not run. 
2.  Speed sensor is not connected. 
3.  Speed sensor is not actuated by the sensor disk 
(check distance). 
-4  Speed variation / VSD ramp up time too long / 
speed below minimum limit for standardization 
Motor has not reached a stable speed after ramp up. 
 
1.  VSD ramp time settings are not shorter than those 
of the LMV37.4 (parameters 522, 523). 
2.  VSD’s characteristic is not linear. Configuration of 
voltage input at the VSD must accord with the 
configuration of the LMV37.4 (DC 0…10 V). 
3.  VSD does not follow quickly enough the change of 
the LMV37.4. Check VSD settings (input filter, 
slippage compensation, hiding various speeds). 
4.  Speed of VSD lies below the minimum for 
standardization (650 rpm). 
-5  Wrong direction of rotation  Motor’s direction of rotation is wrong. 
 
1.  Motor turns in the wrong direction  
 change parameterization of the direction of 
rotation or inter change 2 live conductors. 
2.  Sensor disk is fitted the wrong way  
 turn sensor disk. 
-6  Unplausible sensor signals  The required pulse pattern (60°, 120°, 180°) has not 
been correctly identified. 
 
1.  Speed sensor does not detect all tappets of the 
sensor disk  
 check the distance. 
2.  As the motor turns, other metal parts are detected 
also, in addition to the tappets  
 improve mounting. 
3.  Electromagnetic interference on the sensor lines  
 check cable routing, improve EMC. 
-7  Invalid standardized speed  Standardized speed measured does not lie in the 
permissible range