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ABB DCS550 - Page 291

ABB DCS550
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291
Fault tracing
3ADW000379R0501 DCS550 Manual e e
7-segment
display
Text on DCS
Control Panel
and DWL
Definition / Action
Fault-
word
Fault is
active when
Triplevel
analog tacho: tacho itself, tacho polarity and voltage,
alignment, cabling, coupling, mechanical distu
rbances,
jumper S1 on SDCS-CON-F
EMF: connection converter - armature circuit closed
SDCS-CON-F
F523
523 ExtFanAck
External fan acknowledge missing:
Check:
MotFanAck (10.06)
external fan contactor
external fan circuit
external fan supply voltage
used digital inputs and outputs (group 14)
9.02,
bit 6
RdyRun = 1
4
F524
524 MainContAck
Main contactor acknowledge missing:
Check:
MainContAck (10.21)
MainContCtrlMode (21.16)
switch on - off sequence
auxiliary contactor (relay) switching the main contactor
after On/Off command
safety relays
used digital inputs and outputs (group 14)
9.02,
bit 7
RdyRun = 1
3
F525
525 TypeCode
Type code mismatch:
Check:
TypeCode (97.01)
9.02,
bit 8
always
1
F526
526 ExternalDI
External fault via binary input:
There is no problem with the drive itself!
Check:
ExtFaultSel (30.31)
9.02,
bit 9
Always or
RdyRun = 1
1
F528
528 FieldBusCom
Fieldbus communication loss:
F528
FieldBusCom is only activated after the first data
set from the overriding control is received by the drive.
Before the first data
set is received, only A128
FieldBusCom
is active. The reason is to suppress
unnecessary faults (the start up of the overriding control is
usually slower than the one of the drive).
Check:
CommandSel (10.01), ComLossCtrl (30.28), FB
TimeOut (30.35), CommModule (98.02)
parameter settings of group 51 (fieldbus)
fieldbus cable
fieldbus termination
fieldbus adapter
9.02,
bit 11
always if FB
TimeOut
(30.35)
0
5
F531
531 MotorStalled
Motor stalled:
The
motor torque exceeded StallTorq (30.03) for a time
longer than
StallTime (30.01) while the speed feedback
was below
StallSpeed (30.02). Check:
motor stalled (mechanical couplings of the motor)
proper conditions of load
correct field current
parameter settings of group 20 (limits: current and
torque limits)
9.02,
bit 14
RdyRef = 1
3
F532
532
MotOverSpeed
Motor overspeed:
Check:
9.02,
bit 15
always
3

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