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MIMAKI JV3-160SP - Page 42

MIMAKI JV3-160SP
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– 3.4 –
ERROR20 I/F BOARD
ERROR21 I/F NONE
ERROR23 HOST I/F
ERROR24 I/F INITIAL
ERROR30 OPERATION
ERROR34 DATA REMAIN
ERROR37
HAED_POSITION
* 75SPII, 130SPII only
ERROR40 MOTOR X
ERROR41 MOTOR Y
ERROR42 X CURRENT
ERROR43 Y CURRENT
•A error occurred in
communication between the
main PCB and the interface
board.
The I/F board could not be
recognized.
•A time limit exceeded error
occurred in communication
between the host computer
and the interface board.
The I/F board is in abnormal
conditions.
Improper operation has been
performed.
Operating condition is tried to
be changed when data that has
not yet been plotted remains.
Adjustment of head angle and
head unit were enforced while
the head is set high.
The X-axis motor has been
overloaded.
The Y-axis motor has been
overloaded.
The brush of motor is in
abnormal conditions.
Overcurrent error has arisen
on the X-axis motor
Overcurrent error has arisen
on the Y-axis motor
1) Replace the I/F PCB with a
new one.
2) Replace the main PCB with a
new one.
3) Replace the I/F connection
board with a new one.
4) Supply power to the 1394 PCI
board in the PC through the
power cable.
1) Is the I/F board mounted
correctly ?
1) Is the cable loose?
2) Has an error occurred on the
host computer?
3) Is the application being used
running normally?
1) Replace the I/F PCBwith a
new one.
2) Replace the main PCB with a
new one.
3) Replace the main PCB with a
new one.
1) Indicate the improper
operation.
2) Replace a key board.
3) Replace a main PCB.
1) This tells that any of the
operating conditions cannot be
changed if data that have not
been plotted remains.
1) Put the head position down.
1) Replace X axis motor.
2) Replace a main PCB.
1) Clean the main guide axis.
2) Execute an error maintenance
flow for Y motor.
3) Replace a main PCB.
1) Replace X axis motor.
2) Replace a main PCB.
1) Execute an error maintenance
flow for Y motor.
2) Replace a main PCB.
Message Description
Corrective measures and
recovering procedures

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