What to doCause
Event name /
Aux. code
Code
(hex)
“Y YY” specifies through which BCU
control unit channel the fault was
received.
Check supply cabling, fuses and
switchgear.
Intermediate circuit DC voltage is not
sufficient because of a missing supply
DC link
undervoltage
3220
With parallel-connected modules, check
the auxiliary code (format XXXY YYZZ).
phase, blown fuse or fault in the rectifier
bridge.
“Y YY” specifies through which BCU
control unit channel the fault was
received.
Check the condition of the supply
(voltage, cabling, fuses, switchgear).
Automatic restart failed (see section
Automatic restart (page 82)).
Standby
timeout
3280
Check the auxiliary code (format XXXY
YYZZ). “XXX” specifies the source of the
Difference in DC voltages between
parallel-connected inverter modules.
DC voltage
difference
3291
first error (see “YYY”). “YYY” specifies
the module through which BCU control
unit channel the fault was received (1:
Channel 1, 2: Channel 2, 4: Channel 3,
8: Channel 4, …, 800: Channel 12).
Connect motor cable.Motor circuit fault due to missing motor
connection (all three phases are not
connected).
Output phase
loss
3381
For more information, check the auxiliary
code.
Autophasing routine (see section
Autophasing (page 64)) has failed.
Autophasing3385
Check that the motor ID run has been
successfully completed.
Clear parameter 98.15 Position offset
user.
Check the setting of parameter 99.3
Motor type.
Check the signs of measured and
estimated speeds.
Estimated and measured positions
have opposite signs.
0001
Reverse encoder cable phasing or edit
parameter 99.16.
Check that the load torque is not too
high for the Turning mode (must be
less than 5%).
Check that the motor is not already
rotating when the autophasing routine
starts.
Motor is rotating during autophasing.0002
Check that encoder is not slipping.Too much difference between
measured and estimated positions.
0003
Check parameter 98.15 several times
to verify that the autophasing routine
gives consistent results.
Check the motor model parameters.
Check that the zero pulses are given
correctly.
Rotor did not rotate as expected
between zero pulses.
0004
Check that the selected mode
(parameter 21.13) is appropriate for
the motor.
Position estimate did not stabilize.0005
544 Fault tracing