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Cessna 182 1978 - Slip Ring Alignment; Timer Test; Trouble Shooting

Cessna 182 1978
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MODEL
182
&
T182
SERIES
SERVICE
MANUAL
14-59.
TROUBLE
SHOOTING.
NOTE
The
propeller
de-ice
ammeter
may
be
used
while
trouble
shooting
the
system.
The
ammeter
needle
should
rest
within
the
shaded
band
for
90
seconds
while
the
system
is
heating,
and
then
to
zero
for
90
seconds
while
the
system
is
off.
TROUBLE
PROBABLE
CAUSE
REMEDY
ELEMENTS
DO
NOT
Circuit
breaker
out
or
Reset
circuit
breaker.
If
HEAT.
defective,
it
pops
out
again,
deter-
mine
cause
and
correct.
Defective
wiring.
Repair
or
replace
wiring.
Defective
switch.
Replace
switch.
Defective
timer.
Replace
timer.
Defective
brush-to-
Check
alignment.
Replace
slip
ring
connection.
defective
parts.
CYCLING
SEQUENCE
Crossed
Connections
Correct
wiring.
NOT
CORRECT
OR
NO
CYCLING.
Defective
timer.
Replace
timer.
RAPID
BRUSH
WEAR.
Brush
block
or
slip
Align
properly.
FREQUENT
BREAK-
ring
out
of
align-
AGE.
SCREECHING
ment.
OR
CHATTERING.
14-60.
TIMER
TEST.
NOTE
a.
Remove
connector
plug
of
wire
harness
from
timer
and
jump
power
input
socket
of
wire
harness
Excessive
slip
ring run-out
will
result
in
to
timer
input
pin.
(Refer
to
chart
following
this
severe
arcing
between
the
slip
ring
and
paragraph
for
pin
identification.)
brushes
and
cause
rapid
brush
wear.
If
b.
Jumptimer
ground
pin
to
ground.
allowed
to
persist,
this
condition
will
c.
Turn
on
de-ice
system.
result
in
rapid
deterioration
of
the
slip
d.
Check
timer
operation per
the
chart.
(Use
a
ring
and
brush
contact
surfaces,
leading
voltmeter.
)
to
eventual
failure
of
the
de-ice
system.
e.
Check
volts
to
ground
in
each
case.
If
engine
is
not
running,
and
auxiliary
power
is
not
used.
voltage
a.
Securely
attach
dial
indicator
gage
to
engine.
will
be
battery
voltage
and
cycle
time
may
be
slightly
and
place
pointer
on
slip
ring.
longer
than
indicated.
b.
Rotate
propeller
slowly
by
hand.
noting
the
f.
Hold
voltmeter
probe
on
the
pin
until
the
voltage
deviation
of
the
slip
ring
from
a
true
plane
as
indi-
drops
to
0.
Move
the
probe
to
the
next
pin
in
the
cated
on
the
gage.
sequence
shown
in
the
chart.
Check
voltage
at
each
c.
Check
that
total
run-out
does
not
exceed
0.
008-
pin
in
sequence.
inch
(±0.
004-inch).
Also
check
that
run-out
does
not
exceed
0.
002-inch
within
any
4-inches
of
slip
ring
TIMER
P/N
.............
3E1899-1
travel.
POWER
INPUT
PIN
.
.
......
.
B
(28VDC)
....
GROUND
PIN
....
(28VDC)..
OUTPUT
PIN
............
C
(28VDC)
TIME
REPEAT
CYCLE
TIME
(SECONDS)
...
.90
Due
to
the
loose
fit
of
some
propeller
thrust
bearings,
a
considerable
error
14-61.
SLIP
RING
ALIGNMENT.
After
installation,
may
be
indicated
in
the
readings
by
the
slip
ring
assembly
must
be
checked
for
run-out,
pushing
in
or
pulling
out
on
the
pro-
and
adjustments
made.
if
necessary.
peller
while
rotating
it.
Care
must
be
taken
to
exert
a
uniform
push
or
pull
on
the
propeller
to
hold
this
error
to
a
minimum.
14-19

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