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Siemens SINAMICS G150 - Page 1502

Siemens SINAMICS G150
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4 Faults and alarms
4.2 List of faults and alarms
SINAMICS G130/G150
1502 List Manual (LH2), 04/2014, A5E03263479A
For fault value = 1:
- If required change the motor holding brake configuration (p1215 = 1, 2).
- If this fault value unexpectedly occurs, then the motor connections should be checked in order to rule out that they
have been interchanged.
For fault value = 11:
For a parallel connection, only connect one motor holding brake.
For fault value = 12:
Check the setting of the power unit data set for a parallel connection (p7015).
For fault value = 13:
Before changing p7015, deactivate the "Safe brake control" function (SBC) (p9602).
For fault value = 14:
Check whether the power unit supports the brake control for a parallel connection (r9771.14).
Check whether there is a DRIVE-CLiQ communication error between the Control Unit and the power unit involved
and, if required, carry out a diagnostics routine for the faults identified.
See also: p1215 (Motor holding brake configuration)
Reaction upon N: NONE
Acknowl. upon N: NONE
F07937 (N) Drive: Speed deviation between motor model and external speed
Message value: -
Message class: Application / technological function faulted (17)
Drive object: VECTOR_G
Reaction: OFF2 (NONE, OFF1, OFF3)
Acknowledge: IMMEDIATELY
Cause: The absolute value of the speed difference from the two actual values (r2169, r1443) exceeds the tolerance threshold
(p3236) for longer than permitted (p3238).
Possible causes:
- the interconnection or scaling of the external encoder signal is incorrect (p1440, p2000).
- speed encoder for external encoder signal faulty.
- encoder signal's polarity or gain incorrect.
- smoothing time constant for model speed for monitoring too high (p2157).
- smoothing time constant or threshold values for monitoring too low (p3236, p3238).
If an external encoder signal is not being used:
- check speed signal r0061. For significant signal ripple, check the speed encoder and if required increase p0492.
See also: p2149 (Monitoring configuration)
Remedy: - check that the external speed matches the motor speed (p1440, r1443).
- check the polarity of the external speed (r1443).
- check the interconnection of the connector input and the scaling of the signal (p1440, p2000).
Reaction upon N: NONE
Acknowl. upon N: NONE
F07940 Sync-line-drive: Synchronizing error
Message value: -
Message class: Application / technological function faulted (17)
Drive object: VECTOR_G
Reaction: OFF2
Acknowledge: IMMEDIATELY
Cause: After synchronization has been completed, the phase difference (r3808) is greater than the threshold value, phase
synchronism (p3813).
OFF1 or OFF3 response, while the closed-loop phase control is active (r3819.6 = 1) or synchronism reached
(r3819.2 = 1).
Enable signal withdrawn (p3802 = 0), while the closed-loop phase control was active (r3819.6 = 1).
Remedy: If required increase the threshold value phase synchronism (p3813) for synchronizing the line supply to the drive.
Before OFF1 or OFF3, complete synchronizing (r03819.0 = 0).
Before withdrawing the enable signal (p3802 = 0), reach synchronism (r3819.2 = 1).
See also: p3813 (Sync-line-drive phase synchronism threshold value)

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