Firmware ≤ 05.00 - DMS 4.2 EN - 02/2010 L 469
8400 HighLine | Parameter setting & configuration
Diagnostics & error management
Maloperation of the drive
 
Motor consumes too 
much current
U
min
 boost has been selected too high Correct setting with C00016
V/f base frequency has been selected too low Correct setting with C00015
Rated motor data (stator resistance, speed, 
current, frequency, voltage) and cos ϕ  and/
or magnetising inductance is not adapted to 
the motor data
Carry out automatic motor parameter 
identification with the C00002/23
 controller 
command
- or -
Adjust motor parameters manually:
C00084
: Motor stator resistance
C00087
: Rated motor speed
C00088
: Rated motor current
C00089
: Rated motor frequency
C00090
: Rated motor voltage
C00091
: Motor cosine phi
C00092
: Motor magnetising inductance
Motor parameter 
identification is 
aborted with error 
LP1
Motor is too small compared to the rated 
device power (>1 : 3)
Use device with lower rated power
DC injection brake (DCB) is active via 
terminal
Deactivate DC injection brake
Drive behaviour with 
vector control is not 
satisfactory
different Optimise or manually adapt vector control
Carry out automatic motor parameter 
identification with the C00002/23
 controller 
command
Torque dip in field 
weakening range
or
motor stalling when 
being operated in the 
field weakening 
range
Motor is overloaded Check motor load
Motor windings are wired incorrectly Reverse from star connection to delta 
connection
V/f reference point is set too high Correct setting with C00015
Override point of field weakening is set too 
low
Correct setting with C00080
Mains voltage is too low Increase mains voltage
An asynchronous 
motor with feedback 
rotates without 
control and with too 
low speed
Motor phases have been interchanged
 • Thus the rotating field of the motor is not 
identical anymore with the rotating field 
of the feedback system.
 • Therefore, the drive shows the following 
behaviour if V/f characteristic control 
(C00006
=7) is performed:
–The motor rotates faster than the speed 
setpoint by the value set in C00074
.
–After the controller has been enabled, 
the controller will not stop if the speed 
setpoint = 0 or a quick stop (QSP) occurs.
–Among other things, the final motor 
current depends on the value set for the 
V
min
 boost and may rise up to I
max
 which 
can trigger the "OC5: Ixt overload" fault 
message.
Check the phase position of the motor cable
If possible: Operate the motor with 
deactivated feedback (C00006
=6) and check 
direction of rotation of the motor
Motor phase (LP1) 
monitoring does not 
respond if the motor 
phases are 
interrupted
Monitoring is not active (C00597
= 0) Activate monitoring (C00597 =1)
Maloperation Cause Remedy
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