List of faults and alarms
Faults and alarms
3-1067
© Siemens AG 2012 All Rights Reserved
SINAMICS S110 List Manual (LH7), 06/2012, 6SL3097-4AP10-0BP3
Reaction upon N: NONE
Acknowl. upon N: NONE
Reaction upon A: NONE
Acknowl. upon A: NONE
F07404 Drive: Upper DC link voltage threshold reached
Message value: -
Drive object: SERVO_S110-CAN, SERVO_S110-DP, SERVO_S110-PN
Reaction: OFF2 (NONE, OFF1, OFF3)
Acknowledge: IMMEDIATELY
Cause: The DC link voltage monitoring is active (p1240 = 4, 6) and the upper DC link voltage threshold (p1244) was reached
in the "Operation" state.
Remedy: - check the line supply voltage.
- check the infeed module or the Braking Module.
- increase the upper DC link voltage threshold (p1244).
- switch out (disable) the DC link voltage monitoring (p1240 = 0).
F07410 Drive: Current controller output limited
Message value: -
Drive object: SERVO_S110-CAN, SERVO_S110-DP, SERVO_S110-PN
Reaction: OFF2 (NONE, OFF1)
Acknowledge: IMMEDIATELY
Cause: The condition "I_act = 0 and Uq_set_1 longer than 16 ms at its limit" is present and can be caused by the following:
- motor not connected or motor contactor open.
- no DC link voltage present.
- Motor Module defective.
Remedy: - connect the motor or check the motor contactor.
- check the DC link voltage (r0070).
- check the Motor Module.
F07411 Drive: Flux controller output limited
Message value: -
Drive object: SERVO_S110-CAN, SERVO_S110-DP, SERVO_S110-PN
Reaction: OFF2 (NONE, OFF1)
Acknowledge: IMMEDIATELY
Cause: The specified flux setpoint cannot be reached although 90% of the maximum current has been specified.
- incorrect motor data.
- motor data and motor configuration (star-delta) do not match.
- the current limit has been set too low for the motor.
- induction motor (encoderless, open-loop controlled) in I2t limiting.
- the Motor Module is too small.
Remedy: - correct the motor data.
- check the motor configuration.
- correct the current limits (p0640, p0323).
- reduce the induction motor load.
- if required, use a larger Motor Module.
F07412 Drive: Commutation angle incorrect (motor model)
Message value: -
Drive object: SERVO_S110-CAN, SERVO_S110-DP, SERVO_S110-PN
Reaction: ENCODER (NONE, OFF2)
Acknowledge: IMMEDIATELY
Cause: An incorrect commutation angle was detected that can result in a positive coupling in the speed controller.
Possible causes:
- the motor encoder is incorrectly adjusted with respect to the magnet position.
- the motor encoder is damaged.
- the angular commutation offset is incorrectly set (p0431).