SINAMICS G130/G150
List Manual (LH2), 07/2016, A5E03263479A
1543
4 Faults and alarms
4.2 List of faults and alarms
F07330 Flying restart: Measured search current too low
Message value: -
Message class: Application/technological function faulted (17)
Drive object: VECTOR_G
Component: None Propagation: GLOBAL
Reaction: OFF2 (NONE, OFF1)
Acknowledge: IMMEDIATELY
Cause: During a flying restart, it was identified that the search current reached is too low.
It is possible that the motor is not connected.
Remedy: Check the motor feeder cables.
F07331 Flying restart: Function not supported
Message value: -
Message class: Error in the parameterization / configuration / commissioning procedure (18)
Drive object: VECTOR_G
Component: None Propagation: GLOBAL
Reaction: OFF2 (NONE, OFF1)
Acknowledge: IMMEDIATELY
Cause: It is not possible to power up with the motor rotating (no flying restart).
In the following cases, the "flying restart" function is not supported:
Permanent-magnet synchronous motor (PMSM):
- operation with U/f characteristic.
- encoderless operation without a Voltage Sensing Module (VSM) being connected.
Separately excited synchronous motor (SESM):
- operation with U/f characteristic.
Remedy: - deactivate the "flying restart" function (p1200 = 0).
- change the open-loop/closed-loop control mode (p1300).
- connect a Voltage Sensing Module (VSM) (voltage measurement).
N07332 Flying restart: maximum speed reduced
Message value: %1
Message class: Error in the parameterization / configuration / commissioning procedure (18)
Drive object: VECTOR_G
Component: None Propagation: GLOBAL
Reaction: NONE
Acknowledge: NONE
Cause: The maximum speed that can be reached is reduced; at very high speeds problems associated with the flying restart
can be encountered.
Possible causes:
- power ratio, power unit/motor too high
Remedy: Parameter changes are not required.
Note:
A flying restart at speeds above 3000 rpm should be avoided.
A07350 (F) Drive: Measuring probe parameterized to a digital output
Message value: %1
Message class: Error in the parameterization / configuration / commissioning procedure (18)
Drive object: All objects
Component: None Propagation: LOCAL
Reaction: NONE
Acknowledge: NONE
Cause: The measuring probe is connected to a bi-directional digital input/output and the terminal is set as output.
Alarm value (r2124, interpret decimal):
8: DI/DO 8 (X122.9/X132.1)
9: DI/DO 9 (X122.10/X132.2)